U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/16/2007 - 03/19/2007 ** EVENT NUMBERS ** | !!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!! | Power Reactor | Event Number: 43207 | Facility: SAN ONOFRE Region: 4 State: CA Unit: [ ] [2] [3] RX Type: [1] W-3-LP,[2] CE,[3] CE NRC Notified By: SUSAN GARDNER HQ OPS Officer: JOE O'HARA | Notification Date: 03/02/2007 Notification Time: 17:03 [ET] Event Date: 03/02/2007 Event Time: 10:14 [PST] Last Update Date: 03/16/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.73 - FITNESS FOR DUTY | Person (Organization): DALE POWERS (R4) THEODORE QUAY (NRR) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 99 | Power Operation | 99 | Power Operation | 3 | N | Y | 98 | Power Operation | 98 | Power Operation | Event Text FITNESS FOR DUTY - LICENSED EMPLOYEE A licensed employee had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been revoked. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector. * * * RETRACTION PROVIDED BY S.GARDNER TO KOZAL ON 3/16/07 1728 EDT * * * The licensee provided a retraction regarding the above positive alcohol fitness-for-duty test. Contact the Headquarters Operations Officer for additional details. The licensee notified the NRC Resident Inspector. R4DO (Shannon) notified. | !!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!! | Hospital | Event Number: 43229 | Rep Org: SIBLEY MEMORIAL HOSPITAL Licensee: SIBLEY MEMORIAL HOSPITAL Region: 1 City: WASHINGTON State: DC County: License #: 08-07398-03 Agreement: N Docket: NRC Notified By: JORDIE KECK HQ OPS Officer: JASON KOZAL | Notification Date: 03/12/2007 Notification Time: 13:57 [ET] Event Date: 03/12/2007 Event Time: 12:00 [EDT] Last Update Date: 03/13/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 35.3045(a)(1) - DOSE <> PRESCRIBED DOSAGE | Person (Organization): CHRIS HOTT (R1) SANDRA WASTLER (FSME) | Event Text INCORRECT RADIONUCLIDE ADMINISTERED TO PATIENT The licensee was performing a gall bladder study that required a dose of 5 millicuries of Tc-99 to be administered. A participant in the study was given the wrong radionuclide Gallium Citrate (Ga-67), accelerator produced, in error. Both syringes containing the doses were located in the same case, which was delivered to Sibley Hospital by Mallinckrodt. The licensee informed the patient of the error and that there is minimal risk of adverse effects to the patients health. The actual dose versus the prescribed dose is still under investigation. Additional corrective actions will be determined at a later date. * * * UPDATE 0900 EDT ON 3/13/07 FROM JORDIE KECK TO S. SANDIN * * * The licensee is retracting this report after conducting a review that concluded no reporting criteria was met. Notified R1DO (Hott) and FSME (Morell). A "Medical Event" may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient. | General Information or Other | Event Number: 43230 | Rep Org: LOUISIANA RADIATION PROTECTION DIV Licensee: BAYOU INSPECTION SERVICES Region: 4 City: AMELIA State: LA County: License #: LA-7112-L01 Agreement: Y Docket: NRC Notified By: RICHARD PENROD HQ OPS Officer: JOHN MacKINNON | Notification Date: 03/12/2007 Notification Time: 15:17 [ET] Event Date: 12/31/2006 Event Time: 12:00 [CDT] Last Update Date: 03/12/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): MICHAEL SHANNON (R4) SANDRA WASTLER (FSME) | Event Text AGREEMENT STATE REPORT -TWO OVEREXPOSURES This Agreement State report was received from the State of Louisiana via facsimile. "Bayou Inspection Services reported an overexposure [of] two employees. (Deleted) received an annual dose of 5055 mR. (Deleted) received an annual dose of 5330 mR. Radiation Safety Officer stated he talked to both employees and told them they must do a better job of protecting themselves from exposure to radiation." Event Report ID No.: LA070004 | General Information or Other | Event Number: 43237 | Rep Org: OHIO BUREAU OF RADIATION PROTECTION Licensee: UNKNOWN Region: 3 City: STRONGSVILLE State: OH County: License #: UNKNOWN Agreement: Y Docket: NRC Notified By: STEVEN JAMES HQ OPS Officer: JASON KOZAL | Notification Date: 03/14/2007 Notification Time: 19:34 [ET] Event Date: 03/12/2007 Event Time: 15:00 [EDT] Last Update Date: 03/14/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): RICHARD SKOKOWSKI (R3) JOSEPH GIITTER (FSME) ILTAB VIA E-MAIL () | This material event contains a "Less than Cat 3" level of radioactive material. | Event Text AGREEMENT STATE REPORT - LOST/STOLEN EXIT SIGNS The State provided the following information via email: "On 3/14/07 the Strongsville Ohio Police Department was notified that ten (10) tritium exit signs were missing and presumed stolen from a storage area at a local shopping center construction site. The apparent theft occurred between 3 PM on 3/12/07 and 1 PM on 3/13/07. The contractor reporting the incident stated that the signs could have been taken by anyone that had access to the construction site, because many different contractors were using the same storage area. The ten signs were all packaged in one box. The signs are manufactured by SRB Technologies as the Betalux-E Life Safety Sign, Model 171. They are distributed by Cooper Lighting under the name Sure Lites, TRX1 series. The signs are rated for a 20-year life cycle." Ohio event # - OH70003 THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. This source is not amongst those sources or devices identified by the IAEA Code of Conduct for the Safety & Security of Radioactive Sources to be of concern from a radiological standpoint. Therefore is it being categorized as a less than Category 3 source | Power Reactor | Event Number: 43243 | Facility: GINNA Region: 1 State: NY Unit: [1] [ ] [ ] RX Type: [1] W-2-LP NRC Notified By: KYLE GARNISH HQ OPS Officer: PETE SNYDER | Notification Date: 03/17/2007 Notification Time: 02:13 [ET] Event Date: 03/16/2007 Event Time: 22:09 [EDT] Last Update Date: 03/17/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): CHRIS HOTT (R1) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP CAUSED BY SAFETY INJECTION SIGNAL At 2209 on 3/16/07, the plant tripped on a Safety Injection (SI) signal initiated because of low main steam line pressure in the 'A' main steam loop. The licensee is currently conducting a post trip review but believes that the low main steam line pressure in 'A' loop was caused by a spurious isolation of the 'B' Main Steam Line Isolation Valve (MSIV). The isolation in the 'B' main steam loop lead to high main steam flow and low main steam line pressure in the 'A' main steam loop. The 'A' MSIV then also auto-closed on the SI signal. The plant is currently stable in Mode 3 at about 2235 psig pressure and 547 degrees average Reactor Coolant System (RCS) temperature. All control rods fully inserted on the trip. Decay heat is currently being removed by auxiliary feedwater feeding the steam generators and steaming out the plant atmospheric steam valves. Since plant pressure did not decrease below 1500 psig, SI did not actually inject into the RCS. The licensee secured SI. No primary PORV's or safety valves lifted. No main steam safeties lifted according to plant closure indicators. There are no primary to secondary steam generator tube leaks. All electrical safeguards buses are powered by offsite power. The Emergency Diesel Generators (EDG) started but did not load and were shut down. The EDGs are operable and available if needed. The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 43245 | Facility: PILGRIM Region: 1 State: MA Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: DAVID NOYES HQ OPS Officer: JOHN MacKINNON | Notification Date: 03/17/2007 Notification Time: 21:11 [ET] Event Date: 03/17/2007 Event Time: 16:58 [EDT] Last Update Date: 03/17/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): CHRIS HOTT (R1) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Hot Shutdown | 0 | Hot Shutdown | Event Text GROUP ISOLATIONS FOLLOWING MANUAL REACTOR SCRAM "On March 17 2007, at approximately 1658 EDT, Group 2 (Reactor Building Ventilation Isolation) and Group 6 (RWCU Isolation) automatic containment isolation signals were received due to low reactor water level following the insertion of a manual scram signal. The manual scram signal was inserted following the reaching of internal administrative limits on changes in unidentified drywell leakage. The receipt of these isolation signals is not unusual following the insertion of a scram signal. "The reactor was manually shutdown due to reaching internal administrative limits on changes in unidentified drywell leakage. Prior to the manual shutdown, the leakage had not reached the applicable Technical Specification limits. Drywell leakage as of 1800 EDT was 1.3 GPM identified and 2.59 GPM unidentified with the unit in Hot Shutdown Mode. "All safety systems responded as expected. The plant is in a stable condition. Investigation is continuing." The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 43246 | Facility: MONTICELLO Region: 3 State: MN Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: RANDY SAND HQ OPS Officer: JEFF ROTTON | Notification Date: 03/18/2007 Notification Time: 04:41 [ET] Event Date: 03/17/2007 Event Time: 23:46 [CDT] Last Update Date: 03/18/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): RICHARD SKOKOWSKI (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Refueling | 0 | Refueling | Event Text RPS TRIP SIGNAL AND CONTAINMENT ISOLATIONS RECEIVED DURING MAINTENANCE "With the plant in refueling outage with all rods in and in Mode 5, a RPS trip and a containment isolation was received at 2347, 03/17/07. This event occurred when Div #2 Bus 16 Bus Pot Drawer was opened during isolation of 1AR Transformer Metering under C/O-17605. The opening of this Pot Drawer caused Div #2 4KV Bus 16, Div #2 480V LC-104 and Div #2 480V MCC-141, 142, 143, and 144 to open. 'B' RPS tripped causing full RPS trip due to SRM shorting removed. The loss of power caused RBV [Reactor Building Ventilation] and Spent Fuel Pool Radiation Monitors to trip and cause containment isolation to occur. Investigation into C/O-17605, restoration of power, resetting of RPS and containment isolation in progress." The containment valves that received an isolation signal were: Primary Containment Atmosphere Control, Post Accident H2/O2 Control system, Post Accident Sampling system, O2 analyzing and SCTMT isolation (H&V). The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 43247 | Facility: DUANE ARNOLD Region: 3 State: IA Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: HANS OLSON HQ OPS Officer: BILL HUFFMAN | Notification Date: 03/18/2007 Notification Time: 22:07 [ET] Event Date: 03/18/2007 Event Time: 19:40 [CDT] Last Update Date: 03/18/2007 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): RICHARD SKOKOWSKI (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 28 | Power Operation | 0 | Hot Shutdown | Event Text MANUAL REACTOR SCRAM DUE TO COOLANT CHEMISTRY CONCERNS "This report Is being made under 50.72(b)(2)(iv)(B) for inserting a manual reactor scram due to high levels of reactor coolant chlorides, sulfates, and conductivity. These elevated chemistry parameters may be due to a possible resin intrusion following the placement of a Condensate Demineralizer in service. "In addition, this report is being made under 50.72(b)(3)(iv)(A), 'Any event or condition that results in valid actuation of any systems listed in paragraph (b)(3)(iv)(B) of this section' due to PCIS groups 2, 3, and 4 being received when reactor water level dropped below 170 inches. All isolations went to completion. The reactor water level drop is normal following a scram from 28% power due to void collapse in the reactor vessel. Reactor water level was restored to normal and the PCIS group isolations were reset. "The current plan is to cooldown the plant and enter Mode 4." The scram was characterized as uncomplicated. All rods fully inserted. No safety relief valves lifted. Reactor water low level was approximately 165 inches and was restored with normal reactor feedwater. Decay heat is currently being removed via steam line drains. There were no electrical alignment or grid issues as a result of the transient. No significant Technical Specification LCOs were in effect at the time of the scram. The licensee notified the NRC Resident Inspector. | |