Event Notification Report for August 17, 2001
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
08/16/2001 - 08/17/2001
** EVENT NUMBERS **
38201 38212 38213 38214 38215 38216 38217 38218 38219
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38201 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 08/10/2001|
| UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 23:02[EDT]|
| RXTYPE: [1] GE-2 |EVENT DATE: 08/10/2001|
+------------------------------------------------+EVENT TIME: 21:15[EDT]|
| NRC NOTIFIED BY: ERIC DEMONCH |LAST UPDATE DATE: 08/16/2001|
| HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |DANIEL HOLODY R1 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 84 Power Operation |84 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNPLANNED REACTOR PROTECTION SYSTEM (RPS) SYSTEM/SAFETY SYSTEM ACTUATIONS |
| WHILE CRITICAL |
| |
| The following text is a portion of a facsimile received from the licensee: |
| |
| "[The unit] received [an] isolation of the [transverse incore probe (TIP)] |
| purge system and the offgas system during [an] electrical transient on the |
| 230kV distribution system. [The licensee believes] the isolations were |
| caused by the voltage fluctuations felt in the plant from the grid. Since |
| the TIP purge isolation is processed through [the reactor protection system |
| (RPS)] and offgas from the offgas [radiation] monitors, this falls under |
| actuation of a safety system while critical." |
| |
| "[The licensee] reset isolations and restored systems to normal." |
| |
| The licensee stated that the isolation signals that were processed did not |
| show up on any alarms. Alarms were received but nothing specific to |
| indicate the isolations. This may have been due to voltage |
| fluctuations/losses as a result of power/instrument panels that transferred |
| to their alternate power supplies. The voltage fluctuations on the in-house |
| 4160V buses were attributed to the electrical transient on the 230kV |
| distribution system. |
| |
| There was severe weather in the area at the time of this event. As a |
| result, one of two 230kV outgoing power lines and both 34.5kV feed lines |
| were lost. All of these lines have since been returned to service. The |
| licensee stated that offsite power was never lost because one 230kV line |
| remained available to backfeed/supply the 34.5kV buses. |
| |
| The licensee notified the NRC resident inspector. |
| |
| * * * RETRACTED AT 1840 EDT ON 8/16/2001 BY JERE FREEMAN TO FANGIE JONES * * |
| * |
| |
| The licensee, after review of the event, determined that the actuation of a |
| single component due to a power panel transfer on a voltage transient did |
| not meet the requirement of an actuation of the containment isolation system |
| for reportability. Per NUREG 1022 Rev 2, this event was not reportable and |
| is retracted. |
| |
| The licensee notified the NRC Resident Inspector. The R1DO (William Ruland) |
| has been notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 38212 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MALLINCKRODT INC. |NOTIFICATION DATE: 08/16/2001|
| RXTYPE: NUCLEAR PHARMACY |NOTIFICATION TIME: 10:00[EDT]|
| COMMENTS: RADIOPHARMACEUTICAL OPERATIONS |EVENT DATE: 08/16/2001|
| MEDICAL R&D |EVENT TIME: 08:45[CDT]|
| |LAST UPDATE DATE: 08/16/2001|
| CITY: MARYLAND HTS. REGION: 3 +-----------------------------+
| COUNTY: ST. LOUIS STATE: MO |PERSON ORGANIZATION |
|LICENSE#: 24-4206-01 AGREEMENT: N |THOMAS KOZAK R3 |
| DOCKET: 03000001 |BRIAN SMITH NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: JAMES SCHUH | |
| HQ OPS OFFICER: STEVE SANDIN | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|BAD1 20.2202(a)(1) PERS OVEREXPOSURE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| PERSONNEL OVEREXPOSURES INVOLVING TWO WORKERS BETWEEN 1995 AND 1999 |
| |
| An on-going dose reconstruction in response to Confirmatory Action Letter |
| EA-00-143, dated June 22, 2000, identified two (2) workers who received more |
| than 250 Rem to their extremities, specifically less than one (1) square |
| centimeter of the fingertips. The overexposures occurred between 1995 and |
| 1999 on seven (7) occurrences during the manufacturing process involving |
| P-32. The licensee will inform the two individuals involved and offer |
| medical services, if requested. The licensee discussed this incident with |
| NRC Region 3 (Cameron). |
| |
| * * * UPDATED AT 1532 EDT ON 8/16/2001 BY JAMES SCHUH TO FANGIE JONES * * * |
| |
| The on-going review has identified a total of 4 workers in 10 occurrences |
| with overexposures. All have occurred in similar activities except for 1 |
| person in 2 events doing a different process. NRC Region 3 (Bob Gatone) has |
| been contacted by the licensee. |
| |
| The R3DO (Thomas Kozak) and NMSS (Brian Smith) have been notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38213 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 08/16/2001|
| UNIT: [] [2] [3] STATE: AL |NOTIFICATION TIME: 11:14[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 08/16/2001|
+------------------------------------------------+EVENT TIME: 08:25[CDT]|
| NRC NOTIFIED BY: TERRY KNUETTEL |LAST UPDATE DATE: 08/16/2001|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |CHARLIE PAYNE R2 |
|10 CFR SECTION: | |
|HFIT 26.73 FITNESS FOR DUTY | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 100 Power Operation |100 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| FITNESS FOR DUTY REPORT INVOLVING CONTRACTOR FOREMAN |
| |
| A contractor foreman was determined to be under the influence of alcohol |
| during a random test. The contractor's access to the plant has been |
| terminated. The licensee informed the NRC Region 2 Office (Wallow) and the |
| Resident Inspector. |
| |
| Contact the Headquarters Operation Officer for details. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38214 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 08/16/2001|
| UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 11:40[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/16/2001|
+------------------------------------------------+EVENT TIME: 09:25[EDT]|
| NRC NOTIFIED BY: PETER ORPHANOS |LAST UPDATE DATE: 08/16/2001|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |RONALD BELLAMY R1 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| ALL EMERGENCY OFFSITE SIRENS INOPERABLE |
| |
| The licensee determined that all 16 Emergency Offsite Sirens were |
| inoperable. The exact cause of the failure is unknown and a plan is being |
| developed to repair the sirens. |
| |
| The licensee notified the NRC Resident Inspector and intends to notify the |
| state and local authorities. |
| |
| * * * UPDATED AT 1735 EDT ON 8/16/2001 BY PETER ORPHANOS TO FANGIE JONES * * |
| * |
| |
| "As of 1300 August 16, 2001 163 of 165 Limerick Generating Station Emergency |
| Offsite Sirens are determined to be functional. |
| |
| "A plan has been developed and investigation continues into the cause of the |
| inoperability of the sirens." |
| |
| The licensee notified the NRC Resident Inspector. The R1DO (William Ruland) |
| has been notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 38215 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/16/2001|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 12:23[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/15/2001|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:45[EDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/16/2001|
| CITY: PIKETON REGION: 3 +-----------------------------+
| COUNTY: PIKE STATE: OH |PERSON ORGANIZATION |
|LICENSE#: GDP-2 AGREEMENT: N |THOMAS KOZAK R3 |
| DOCKET: 0707002 |JOHN HICKEY NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: MIKE RITCHIE | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NBNL RESPONSE-BULLETIN | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| 24-HOUR NRC BULLETIN 91-01 REPORT |
| |
| The licensee has notified the NRC Resident Inspector and the DOE |
| representative. |
| |
| The following text is a portion of a facsimile received from Portsmouth |
| personnel: |
| |
| During a walk through of the X-705 Decontamination Facility a hole was |
| discovered on the top of the Calciner glove box. The hole could have allowed |
| uranium bearing solution to accumulate in the bottom of the glove box [in] |
| the unlikely event of a leak. This is in violation of the analysis of |
| NCSA-705_024.E02 "Calciner Solution Recovery" which specifically evaluates |
| this event. |
| |
| The PSS entered an anomalous condition. Tape was placed over the hole on the |
| top of the Calciner glove box. The PSS exited the anomalous condition. |
| |
| This event is reportable per NRC BL 91-01 as a loss of one control of the |
| double contingency principle. |
| |
| SAFETY SIGNIFICANCE OF EVENTS: low |
| |
| There was no leak of uranium bearing material in the vicinity of the |
| Calciner glove box. Also, the opening on the glove box is very small. This |
| would require a significant amount of time for the solution to accumulate in |
| the glove [box] had a leak occurred at that exact location. |
| |
| POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW |
| CRITICALITY COULD |
| OCCUR): |
| |
| For a criticality to occur, the following events would be required: The |
| recovery system would have to be operating and processing uranium bearing |
| liquid with a high concentration of uranium. Then the leak in this system |
| must occur such that solution sprays onto the glove box. The liquid would |
| then have to flow through the small opening on the top of the glove box and |
| accumulate to a depth of >1.5 inches. |
| |
| CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): |
| volume, geometry |
| |
| The unlikely event supporting double contingency credits the integrity of |
| the glove box for preventing solution from collecting in an unsafe |
| geometry/volume. The hole on the top of the glove box could potentially |
| allow solution to enter the glove box. |
| |
| ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS |
| LIMIT AND % WORST CASE OF CRITICAL MASS): |
| |
| No uranium material was involved in this event. |
| |
| NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION |
| OF THE FAILURES OR DEFICIENCIES: |
| |
| The hole could have allowed uranium bearing solution to accumulate in the |
| bottom of the glove box in the unlikely event of a leak. This is in |
| violation of the analysis of NCSA-705_024.E02 "Calciner Solution Recovery" |
| which specifically evaluates this event. The presence of the opening |
| undermines the basis of an unlikely event credited for double contingency. |
| |
| CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS IMPLEMENTED: |
| |
| Tape was [placed] on the hole on top of the glove box. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38216 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 08/16/2001|
| UNIT: [1] [2] [3] STATE: SC |NOTIFICATION TIME: 16:19[EDT]|
| RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 08/16/2001|
+------------------------------------------------+EVENT TIME: 13:55[EDT]|
| NRC NOTIFIED BY: PRESTON GILLESPIE |LAST UPDATE DATE: 08/16/2001|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |CHARLIE PAYNE R2 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 100 Power Operation |100 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE TO OIL SPILL AT ASSOCIATED HYDRO UNIT |
| |
| The licensee was performing work on the pier at the Keowee Hydro Intake |
| structure when about 1 gallon of Mobil EAL 224H (biodegradable) oil spilled |
| into Lake Keowee. A boom had previously been installed and contained the |
| oil in a 50 foot by 50 foot area. The spill was a result of a hydraulic |
| hose leak. The clean-up was nearly complete at the time of the report. |
| There was no effect on plant operations or any safety significance. |
| |
| The licensee notified the National Response Center, the South Carolina |
| Department of Health and Environmental Control, and the NRC Resident |
| Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|General Information or Other |Event Number: 38217 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: COLORADO DEPT OF HEALTH |NOTIFICATION DATE: 08/16/2001|
|LICENSEE: CITY AND COUNTY OF DENVER |NOTIFICATION TIME: 19:00[EDT]|
| CITY: DENVER REGION: 4 |EVENT DATE: 08/14/2001|
| COUNTY: DENVER STATE: CO |EVENT TIME: 13:40[MDT]|
|LICENSE#: 333-03 AGREEMENT: Y |LAST UPDATE DATE: 08/16/2001|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |WILLIAM JOHNSON R4 |
| |THOMAS ESSIG NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: CLAYTON GOODWIN | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - DAMAGED TROXLER GAUGE |
| |
| "At approximately 1:40 PM on August 14, 2001 an unidentified person in a |
| private automobile ran over a Troxler nuclear density gauge while this gauge |
| was being used by a trained technician at a work site southwest Denver. The |
| technician narrowly escaped being stuck by the vehicle, but the vehicle did |
| strike the gauge. The exterior casing of the gauge was damaged and broken |
| into numerous pieces as a result of the collision. However the sealed source |
| and shielding assembly remained intact. Following the incident the source |
| was able to be retracted into the shielding and the shutter closed." |
| |
| Denver Police were notified immediately following the incident. |
| |
| The site and the gauge with the sealed source were surveyed and no leakage |
| was found. |
| |
| The Troxler gauge involved is a model 4640B (serial number 841) containing a |
| single, 8-millicurie, Cs-137, sealed source (serial number 50-7987). |
| |
| The gauge will be shipped back to Troxler. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38218 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 08/17/2001|
| UNIT: [2] [3] [] STATE: PA |NOTIFICATION TIME: 00:31[EDT]|
| RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 08/16/2001|
+------------------------------------------------+EVENT TIME: 23:25[EDT]|
| NRC NOTIFIED BY: STEVE TANNER |LAST UPDATE DATE: 08/17/2001|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |WILLIAM RULAND R1 |
|10 CFR SECTION: | |
|ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 82 Power Operation |82 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS OF EMERGENCY SIREN REMOTE ACTUATION CAPABILITY |
| |
| "Omni phone system was lost resulting in a loss of Emergency Siren remote |
| actuation control. Power was lost 8/16/01 22:25 EDT and restored 8/16/01 |
| 23:55 EDT. Per reportability manual ID# E-02 and Event# SAF 1.10, loss of |
| assessment capability is reportable after 8 hours, but loss of greater than |
| 25% of the sirens for more than one hour constitutes immediate |
| notification. |
| |
| "The omni phone system was lost due to the associated battery voltage |
| becoming too low to support system operation. This was caused by a |
| temporary battery charger installed in place of the normal charger (due to a |
| failed transformer) not maintaining the battery adequately charged. |
| Immediate omni system recovery was effected using available AC power from an |
| alternate source to power up the equipment. Long term plans are to replace |
| the failed transformer and return the normal charger to service." |
| |
| The licensee informed the NRC resident inspector and will inform state/local |
| agencies. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Other Nuclear Material |Event Number: 38219 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: McMINN'S ASPHALT CO., INC. |NOTIFICATION DATE: 08/17/2001|
|LICENSEE: McMINN'S ASPHALT CO., INC. |NOTIFICATION TIME: 04:59[EDT]|
| CITY: MANHEIM REGION: 1 |EVENT DATE: 08/17/2001|
| COUNTY: STATE: PA |EVENT TIME: 00:30[EDT]|
|LICENSE#: 371965901 AGREEMENT: N |LAST UPDATE DATE: 08/17/2001|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |WILLIAM RULAND R1 |
| | |
+------------------------------------------------+ |
| NRC NOTIFIED BY: GARY LUTZ | |
| HQ OPS OFFICER: STEVE SANDIN | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NINF INFORMATION ONLY | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| TROXLER GAUGE DAMAGED BY VEHICLE AT CONSTRUCTION SITE |
| |
| At 0030EDT on 8/17/01 a light pickup truck struck a Troxler gauge at a road |
| construction project on State Road 340 in Lancaster, PA. The East Lampeter |
| Police Department responded (Incident # 01-414) briefly closing traffic. |
| The RSO surveyed the device and confirmed that the sealed source was intact |
| prior to removal. The Troxler is a model 4640B containing an 8-millicurie |
| Cs-137 source. The licensee is returning the device to the manufacturer's |
| service center in Timonium, MD for inspection and repair. |
+------------------------------------------------------------------------------+
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