Event Notification Report for August 6, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           08/03/2001 - 08/06/2001

                              ** EVENT NUMBERS **

38184  38185  38186  38187  

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   38184       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT   |NOTIFICATION DATE: 08/03/2001|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 20:33[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        08/03/2001|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        16:42[EDT]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  08/03/2001|
|    CITY:  PIKETON                  REGION:  3  +-----------------------------+
|  COUNTY:  PIKE                      STATE:  OH |PERSON          ORGANIZATION |
|LICENSE#:  GDP-2                 AGREEMENT:  N  |JOHN MADERA          R3      |
|  DOCKET:  0707002                              |                             |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  RON CRABTREE                 |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NONR                     OTHER UNSPEC REQMNT    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 4-HOUR REPORT INVOLVING NOTIFICATION TO OTHER GOVERNMENT AGENCIES            |
|                                                                              |
| "On 8/3/01 at 1642 the Plant Shift Superintendent received a 911 emergency   |
| response notification of a vehicle accident on perimeter road, which is      |
| included in the Department Of Energy (DOE) reservation. There was one (1)    |
| fatality and three (3) injuries which required hospitalization.              |
| Notifications of the vehicle accident were made to Pike County (Ohio)        |
| Sheriff's Office. Once it was determined that the accident involved a        |
| fatality DOE-OROC, and DOE-HQ were also notified.                            |
|                                                                              |
| "This PORTS notification to 'other government agencies' requires             |
| notification to the NRC as a 4-hour NRC Event Report."                       |
|                                                                              |
| The NRC resident inspector was informed of this report.                      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38185       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PRAIRIE ISLAND           REGION:  3  |NOTIFICATION DATE: 08/03/2001|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 22:56[EDT]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        08/03/2001|
+------------------------------------------------+EVENT TIME:        20:40[CDT]|
| NRC NOTIFIED BY:  JOEL SORENSEN                |LAST UPDATE DATE:  08/04/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNUSUAL EVENT         |JOHN MADERA          R3      |
|10 CFR SECTION:                                 |HERB BERKOW          NRR     |
|AAEC 50.72(a) (1) (i)    EMERGENCY DECLARED     |JOSEPH HOLONICH      IRO     |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|JIM DYER             RA      |
|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|JON JOHNSON          NRR     |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |ZAPATA               FEMA    |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       20       Power Operation  |0        Hot Standby      |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNIT 1 DECLARED AN UNUSUAL EVENT DUE TO A FIRE LASTING GREATER THAN 10       |
| MINUTES                                                                      |
|                                                                              |
| A fire occurred in the 4KV Bus 12  while realigning the electrical power     |
| supplies from the 1 Reserve Transformer to the 1 Main Transformer during     |
| power ascension.  Bus 12 supplies both the 12 Reactor Coolant Pump and the   |
| 12 Feedwater Pump which were secured.  The 11 Reactor Coolant Pump was also  |
| secured placing the unit in natural circulation.  Auxiliary Feedwater Pumps  |
| 11 and 12 are in service (autostarted on lo-lo SG level) supplying both      |
| Steam Generators (SG) as normal for a reactor trip.  The Main Condenser is   |
| in-service for decay heat removal.                                           |
|                                                                              |
| The licensee is in the process of electrically isolating Bus 12.  The Red    |
| Wing Fire Department is onsite responding to the fire which has not been     |
| confirmed extinguished at the time of this report.                           |
|                                                                              |
| The cause of the reactor trip and the fire is unknown.                       |
|                                                                              |
| The licensee informed state/local agencies and the NRC resident inspector.   |
|                                                                              |
| * * * UPDATED AT 0016 EDT ON 8/4/2001 BY SCOTT WHITSON TO FANGIE JONES * *   |
| *                                                                            |
|                                                                              |
| The licensee reported that 2 employees were treated for heat exhaustion on   |
| site and another employee was transported to a local hospital at 2255 CDT    |
| for the same reason.  All were part of the onsite fire brigade.              |
|                                                                              |
| * * * UPDATED AT 0115 EDT ON 8/4/2001 BY DENNIS CARLSON TO FANGIE JONES * *  |
| *                                                                            |
|                                                                              |
| The licensee exited the Unusual Event at 0012 CDT on 8/4/2001.  The plant is |
| stable in natural circulation and all safeguards buses are energized  by     |
| offsite power.  The licensee notified the NRC Resident Inspector.            |
|                                                                              |
| The R3DO (John Madera), NRR EO (Herb Berkow), and FEMA (Zapata) have been    |
| notified.                                                                    |
|                                                                              |
| * * * UPDATED AT 0325 EDT ON 8/4/2001 BY MIKE SLEIGH TO FANGIE JONES * * *   |
|                                                                              |
| The licensee reported that at the beginning of the Unusual Event a           |
| safeguards degradation related to the area boundary took place.              |
| Compensatory measures were taken upon discovery.                             |
|                                                                              |
| The licensee notified the NRC Resident Inspector and intends to notify R3    |
| IAT (James Creed).  The R3DO (John Madera) was notified.                     |
|                                                                              |
| Refer to the HOO Log for details.                                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38186       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DIABLO CANYON            REGION:  4  |NOTIFICATION DATE: 08/04/2001|
|    UNIT:  [1] [2] []                STATE:  CA |NOTIFICATION TIME: 19:55[EDT]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        08/04/2001|
+------------------------------------------------+EVENT TIME:        15:22[PDT]|
| NRC NOTIFIED BY:  DAVID BAHNER                 |LAST UPDATE DATE:  08/04/2001|
|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |CHUCK CAIN           R4      |
|10 CFR SECTION:                                 |HERB BERKOW          NRR     |
|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC START OF BOTH UNITS DIESEL GENERATORS DUE TO A LOSS OF START-UP    |
| POWER                                                                        |
|                                                                              |
| "Electrical fault caused loss of Start-up Power to both units.  This caused  |
| all six [6] diesel generators on both units to automatically start."         |
|                                                                              |
| Circuit breaker CB212 which supplies 230KV start-up power to both units      |
| opened due to an unidentified electrical fault.  Initial indication was a    |
| loss of power to outbuildings onsite followed about twenty-two (22) minutes  |
| later with a loss of power to the Start-up transformers.  Investigation      |
| found the grounding fuses on the Unit 1 side open.  Should a unit trip occur |
| while in this condition, RCS cooldown by natural circulation would be        |
| required.                                                                    |
|                                                                              |
| Both units are in Tech Spec LCO 3.8.1 Condition 'A' which requires           |
| restoration of start-up power within 72-hours or unit shutdown; mode 3 (hot  |
| standby) in the following 6-hours followed by mode 5 (cold shutdown)         |
| 36-hours later.  The licensee is performing a maintenance and engineering    |
| evaluation to determine if start-up can be restored by closing a cross-tie   |
| breaker from Unit 2.                                                         |
|                                                                              |
| None of the diesel generators loaded and all have been secured and returned  |
| to standby.                                                                  |
|                                                                              |
| The licensee informed the NRC resident inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   38187       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HATCH                    REGION:  2  |NOTIFICATION DATE: 08/05/2001|
|    UNIT:  [1] [2] []                STATE:  GA |NOTIFICATION TIME: 22:25[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        08/05/2001|
+------------------------------------------------+EVENT TIME:        21:30[EDT]|
| NRC NOTIFIED BY:  ALAN WOLFE                   |LAST UPDATE DATE:  08/05/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |KERRY LANDIS         R2      |
|10 CFR SECTION:                                 |                             |
|ACOM 50.72(b)(3)(xiii)   LOSS COMM/ASMT/RESPONSE|                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| NOAA WEATHER RADIO SYSTEM INOPERABLE                                         |
|                                                                              |
| The NOAA weather radio system was determined to be inoperable at 2130 EDT.   |
| The radio system is used as part of the licensee's prompt notification       |
| system.  The licensee has contacted state and local government agencies.     |
|                                                                              |
| The NRC resident inspector will be informed of this notification by the      |
| licensee.                                                                    |
+------------------------------------------------------------------------------+


Page Last Reviewed/Updated Thursday, March 25, 2021