Event Notification Report for February 5, 2001

                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           02/02/2001 - 02/05/2001

                              ** EVENT NUMBERS **

37710  37711  37712  37713  37714  37715  37716  

+------------------------------------------------------------------------------+
|Other Nuclear Material                           |Event Number:   37710       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  U.S. ARMY                            |NOTIFICATION DATE: 02/02/2001|
|LICENSEE:  U.S. ARMY                            |NOTIFICATION TIME: 11:13[EST]|
|    CITY:  ROCK ISLAND              REGION:  3  |EVENT DATE:        12/03/2000|
|  COUNTY:                            STATE:  IL |EVENT TIME:             [CST]|
|LICENSE#:  12-00722-06           AGREEMENT:  Y  |LAST UPDATE DATE:  02/02/2001|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |DAVID HILLS          R3      |
|                                                |BLAIR SPITZBERG      R4      |
+------------------------------------------------+BRIAN SMITH          NMSS    |
| NRC NOTIFIED BY:  JEFF HAVENNER                |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|BAB1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| MISSING M67 MORTAR SIGHT DEVICE                                              |
|                                                                              |
| The licensee reported that an M67 Mortar Sight Device was lost in December   |
| 2000 at Ft. Polk, LA during a training exercise for the 2nd Armored Cavalry. |
| The device contains multiple Tritium sources with an aggregate activity of   |
| 5.8 Curies.  The licensee does not believe the device was inadvertently sent |
| to the landfill, however, there are no specific plans to attempt recovery.   |
| The training area is restricted and inaccessible to the general public.      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Fuel Cycle Facility                              |Event Number:   37711       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT      |NOTIFICATION DATE: 02/03/2001|
|   RXTYPE: URANIUM ENRICHMENT FACILITY          |NOTIFICATION TIME: 01:50[EST]|
| COMMENTS: 2 DEMOCRACY CENTER                   |EVENT DATE:        02/02/2001|
|           6903 ROCKLEDGE DRIVE                 |EVENT TIME:        10:30[CST]|
|           BETHESDA, MD 20817    (301)564-3200  |LAST UPDATE DATE:  02/03/2001|
|    CITY:  PADUCAH                  REGION:  3  +-----------------------------+
|  COUNTY:  McCRACKEN                 STATE:  KY |PERSON          ORGANIZATION |
|LICENSE#:  GDP-1                 AGREEMENT:  Y  |DAVID HILLS          R3      |
|  DOCKET:  0707001                              |M. WAYNE HODGES      NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  MIKE UNDERWOOD               |                             |
|  HQ OPS OFFICER:  BOB STRANSKY                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          N/A                   |                             |
|10 CFR SECTION:                                 |                             |
|OCBA 76.120(c)(2)        SAFETY EQUIPMENT FAILUR|                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TWO CRITICALITY ALARM HORNS FAILED TO SOUND DURING TESTING                   |
|                                                                              |
| "At 1030 on 2-2-01 the PSS was informed that the two Criticality Accident    |
| Alarm System (CAAS) pneumatic horns for building C-337-A failed to sound     |
| properly during testing. The system is required to be operable according to  |
| TSR 2.4.4.3.b for the prescribed modes of operation. Even though the system  |
| was declared inoperable at the time of the failure it is possible that the   |
| system would not have performed its intended safety function had it been     |
| required prior to being declared inoperable. The two horns were replaced and |
| satisfactorily tested.                                                       |
|                                                                              |
| "This event is reportable under 10 CFR 76.120(c)(2) as an event in which     |
| equipment required by the TSR is disabled or fails to function as            |
| designed."                                                                   |
|                                                                              |
| The NRC resident inspector has been informed of this event.                  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37712       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MILLSTONE                REGION:  1  |NOTIFICATION DATE: 02/03/2001|
|    UNIT:  [] [] [3]                 STATE:  CT |NOTIFICATION TIME: 03:51[EST]|
|   RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP           |EVENT DATE:        02/03/2001|
+------------------------------------------------+EVENT TIME:        03:40[EST]|
| NRC NOTIFIED BY:  RAY MARTIN                   |LAST UPDATE DATE:  02/03/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DANIEL HOLODY        R1      |
|10 CFR SECTION:                                 |                             |
|*PRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     N          Y       0        Startup          |0        Hot Standby      |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION                                                         |
|                                                                              |
| The licensee contacted offsite government agencies to inform them that the   |
| unit commenced a refueling outage. The NRC resident inspector has been       |
| informed.                                                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37713       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAN ONOFRE               REGION:  4  |NOTIFICATION DATE: 02/03/2001|
|    UNIT:  [] [] [3]                 STATE:  CA |NOTIFICATION TIME: 18:47[EST]|
|   RXTYPE: [1] W-3-LP,[2] CE,[3] CE             |EVENT DATE:        02/03/2001|
+------------------------------------------------+EVENT TIME:        15:27[PST]|
| NRC NOTIFIED BY:  BOB CONOSCENTI               |LAST UPDATE DATE:  02/04/2001|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          UNU                   |BLAIR SPITZBERG      R4      |
|10 CFR SECTION:                                 |RICHARD WESSMAN      NRR     |
|*AEC 50.72(a) (1) (i)    EMERGENCY DECLARED     |CHARLES MILLER       IRO     |
|                                                |GENE NUPP            FEMA    |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|                                                   |                          |
|                                                   |                          |
|3     A/R        Y       39       Power Operation  |0        Hot Standby      |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO FIRE LASTING MORE THAN 15 MINUTES              |
|                                                                              |
| The plant was in the process of raising power after exiting shutdown         |
| operations and were at 39% power when a non-class 1E breaker failed at 1514  |
| PST causing a loss of power to  a non-safety electrical bus.  This in turn   |
| caused the loss of some secondary plant equipment which led to the loss of   |
| condenser vacuum, condensate pumps, feedwater pumps, and other equipment     |
| leading to a trip of the plant.  The breaker failure resulted in a fire      |
| which lasted until 1544 PST and the Unusual Event was declared at 1527 PST.  |
| The plant also lost all the control room annunciators for a period of time,  |
| they have been recovered.  The plant is stable in Hot Standby with the       |
| reactor coolant pumps running, auxiliary feedwater supplying the steam       |
| generators, and excess heat being released through the steam generator       |
| atmospheric dumps.  The main steam isolation valves are closed as a result   |
| of the secondary equipment that was lost.  The emergency diesel generators   |
| were running unloaded on automatic start signal from the loss of the         |
| non-class 1E bus.  Electrical power continues to be provided to all safety   |
| busses and the unaffected parts of the non-safety busses from offsite        |
| power.                                                                       |
|                                                                              |
| The licensee notified the NRC Resident Inspector and state and local         |
| authorities.                                                                 |
|                                                                              |
| * * * UPDATE AT 1956 EST ON 02/03/01 BY BOB CONOSCENTI TO FANGIE JONES * *   |
| *                                                                            |
|                                                                              |
| The licensee has determined that one breaker failed catastrophically causing |
| the loss of one 4160 VAC bus and pieces of the breaker assembly caused       |
| grounds in another 480 VAC bus causing its loss.  The plant is stable in Hot |
| Standby.  The licensee notified the NRC Resident Inspector.  The Unusual     |
| Event was terminated at 1544 PST.                                            |
|                                                                              |
| The R4DO (Blair Spitzberg), NRR EO (Richard Wessman), IRO Manager (Charles   |
| Miller), and FEMA (Gene Nupp) have been notified.                            |
|                                                                              |
| * * * COMMISSIONER'S ASSISTANTS' BRIEFING 1000 2/4/2001 * * *                |
|                                                                              |
| Briefer: Charles Marshall. Participants: Mamish (IRO), Richards, Wessman     |
| (NRR), Dricks (OPA), Combs (STP), Hauber (OIP), Madden (OCA), Morris (EDO),  |
| Levin (Chrm Meserve), Cain (Comm Dicus), Sharkey (Comm McGaffigan), Davis    |
| (Comm Diaz), McCabe (Comm Merrifield), Brockman, Henerson, Kramer (R4).      |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37714       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON                  REGION:  3  |NOTIFICATION DATE: 02/04/2001|
|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 04:25[EST]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        02/04/2001|
+------------------------------------------------+EVENT TIME:        01:18[CST]|
| NRC NOTIFIED BY:  MATT BAKER                   |LAST UPDATE DATE:  02/04/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(ii)     RPS ACTUATION          |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     A/R        Y       96       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| AUTOMATIC TURBINE TRIP/REACTOR SCRAM DURING TESTING                          |
|                                                                              |
| During performance or routine turbine valve testing, an automatic turbine    |
| trip and subsequent reactor scram occurred due to low turbine emergency trip |
| system pressure. The unit is currently stable in Condition 3 (Hot Shutdown)  |
| with reactor vessel water level being maintained by the motor driven         |
| feedwater pump and reactor pressure being controlled via the steam bypass    |
| valves to the main condenser. All systems functioned as expected.            |
|                                                                              |
| The NRC resident inspector has been informed of this event by the licensee.  |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37715       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH              REGION:  3  |NOTIFICATION DATE: 02/04/2001|
|    UNIT:  [1] [] []                 STATE:  WI |NOTIFICATION TIME: 14:52[EST]|
|   RXTYPE: [1] W-2-LP,[2] W-2-LP                |EVENT DATE:        02/04/2001|
+------------------------------------------------+EVENT TIME:        12:45[CST]|
| NRC NOTIFIED BY:  MIKE MEYER                   |LAST UPDATE DATE:  02/04/2001|
|  HQ OPS OFFICER:  FANGIE JONES                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |DAVID HILLS          R3      |
|10 CFR SECTION:                                 |                             |
|*IND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       80       Power Operation  |80       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DISCOVERY OF VALVE CLOSED THAT COULD AFFECT ACCIDENT MITIGATION              |
|                                                                              |
| "While performing troubleshooting operation on the Unit 1 Crossover Steam    |
| Dump System an Instrument Air Valve was discovered to be closed, when it     |
| should have been open.  This closed valve (IA-1553) isolates Instrument Air  |
| to the Crossover Steam Dump Valves rendering the system inoperable.  This    |
| system is required to be operable by the FSAR Appendix T and Power must be   |
| <437 MWe if the system is inop.  At the time of discovery power was <437     |
| MWe, however initial investigation leads to the conclusion that this valve   |
| has probably been closed since October, 2000.  Since Crossover Steam Dumps   |
| provide protection for a Turbine Overspeed Accident and is part of the PBNP  |
| Design Basis it was conservatively decided to make this 8-hour report.  Unit |
| 1 will remain < 437 MWe until the system is fully restored and tested.  An   |
| investigation is continuing."                                                |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   37716       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 02/05/2001|
|    UNIT:  [1] [2] []                STATE:  TX |NOTIFICATION TIME: 05:02[EST]|
|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        02/05/2001|
+------------------------------------------------+EVENT TIME:        03:15[CST]|
| NRC NOTIFIED BY:  STEVEN KASPAR                |LAST UPDATE DATE:  02/05/2001|
|  HQ OPS OFFICER:  BOB STRANSKY                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          N/A                   |BLAIR SPITZBERG      R4      |
|10 CFR SECTION:                                 |                             |
|DDDD 73.71               UNSPECIFIED PARAGRAPH  |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|2     N          Y       9        Power Operation  |9        Power Operation  |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| 10 CFR 73.71(b) SECURITY REPORT                                              |
|                                                                              |
| Safeguards system degradation related to detection/monitoring. Immediate     |
| compensatory measures taken upon discovery. Contact the NRC Operations       |
| Center for additional details.                                               |
|                                                                              |
| The NRC resident inspector will be informed of this event by the licensee.   |
+------------------------------------------------------------------------------+


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