Event Notification Report for February 5, 2001
U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
02/02/2001 - 02/05/2001
** EVENT NUMBERS **
37710 37711 37712 37713 37714 37715 37716
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|Other Nuclear Material |Event Number: 37710 |
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| REP ORG: U.S. ARMY |NOTIFICATION DATE: 02/02/2001|
|LICENSEE: U.S. ARMY |NOTIFICATION TIME: 11:13[EST]|
| CITY: ROCK ISLAND REGION: 3 |EVENT DATE: 12/03/2000|
| COUNTY: STATE: IL |EVENT TIME: [CST]|
|LICENSE#: 12-00722-06 AGREEMENT: Y |LAST UPDATE DATE: 02/02/2001|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |DAVID HILLS R3 |
| |BLAIR SPITZBERG R4 |
+------------------------------------------------+BRIAN SMITH NMSS |
| NRC NOTIFIED BY: JEFF HAVENNER | |
| HQ OPS OFFICER: STEVE SANDIN | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| MISSING M67 MORTAR SIGHT DEVICE |
| |
| The licensee reported that an M67 Mortar Sight Device was lost in December |
| 2000 at Ft. Polk, LA during a training exercise for the 2nd Armored Cavalry. |
| The device contains multiple Tritium sources with an aggregate activity of |
| 5.8 Curies. The licensee does not believe the device was inadvertently sent |
| to the landfill, however, there are no specific plans to attempt recovery. |
| The training area is restricted and inaccessible to the general public. |
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|Fuel Cycle Facility |Event Number: 37711 |
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| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 02/03/2001|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 01:50[EST]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 02/02/2001|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:30[CST]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 02/03/2001|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 |
| DOCKET: 0707001 |M. WAYNE HODGES NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: MIKE UNDERWOOD | |
| HQ OPS OFFICER: BOB STRANSKY | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| TWO CRITICALITY ALARM HORNS FAILED TO SOUND DURING TESTING |
| |
| "At 1030 on 2-2-01 the PSS was informed that the two Criticality Accident |
| Alarm System (CAAS) pneumatic horns for building C-337-A failed to sound |
| properly during testing. The system is required to be operable according to |
| TSR 2.4.4.3.b for the prescribed modes of operation. Even though the system |
| was declared inoperable at the time of the failure it is possible that the |
| system would not have performed its intended safety function had it been |
| required prior to being declared inoperable. The two horns were replaced and |
| satisfactorily tested. |
| |
| "This event is reportable under 10 CFR 76.120(c)(2) as an event in which |
| equipment required by the TSR is disabled or fails to function as |
| designed." |
| |
| The NRC resident inspector has been informed of this event. |
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|Power Reactor |Event Number: 37712 |
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| FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 02/03/2001|
| UNIT: [] [] [3] STATE: CT |NOTIFICATION TIME: 03:51[EST]|
| RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 02/03/2001|
+------------------------------------------------+EVENT TIME: 03:40[EST]|
| NRC NOTIFIED BY: RAY MARTIN |LAST UPDATE DATE: 02/03/2001|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DANIEL HOLODY R1 |
|10 CFR SECTION: | |
|*PRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
| | |
|3 N Y 0 Startup |0 Hot Standby |
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EVENT TEXT
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| OFFSITE NOTIFICATION |
| |
| The licensee contacted offsite government agencies to inform them that the |
| unit commenced a refueling outage. The NRC resident inspector has been |
| informed. |
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|Power Reactor |Event Number: 37713 |
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| FACILITY: SAN ONOFRE REGION: 4 |NOTIFICATION DATE: 02/03/2001|
| UNIT: [] [] [3] STATE: CA |NOTIFICATION TIME: 18:47[EST]|
| RXTYPE: [1] W-3-LP,[2] CE,[3] CE |EVENT DATE: 02/03/2001|
+------------------------------------------------+EVENT TIME: 15:27[PST]|
| NRC NOTIFIED BY: BOB CONOSCENTI |LAST UPDATE DATE: 02/04/2001|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: UNU |BLAIR SPITZBERG R4 |
|10 CFR SECTION: |RICHARD WESSMAN NRR |
|*AEC 50.72(a) (1) (i) EMERGENCY DECLARED |CHARLES MILLER IRO |
| |GENE NUPP FEMA |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
| | |
|3 A/R Y 39 Power Operation |0 Hot Standby |
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EVENT TEXT
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| UNUSUAL EVENT DECLARED DUE TO FIRE LASTING MORE THAN 15 MINUTES |
| |
| The plant was in the process of raising power after exiting shutdown |
| operations and were at 39% power when a non-class 1E breaker failed at 1514 |
| PST causing a loss of power to a non-safety electrical bus. This in turn |
| caused the loss of some secondary plant equipment which led to the loss of |
| condenser vacuum, condensate pumps, feedwater pumps, and other equipment |
| leading to a trip of the plant. The breaker failure resulted in a fire |
| which lasted until 1544 PST and the Unusual Event was declared at 1527 PST. |
| The plant also lost all the control room annunciators for a period of time, |
| they have been recovered. The plant is stable in Hot Standby with the |
| reactor coolant pumps running, auxiliary feedwater supplying the steam |
| generators, and excess heat being released through the steam generator |
| atmospheric dumps. The main steam isolation valves are closed as a result |
| of the secondary equipment that was lost. The emergency diesel generators |
| were running unloaded on automatic start signal from the loss of the |
| non-class 1E bus. Electrical power continues to be provided to all safety |
| busses and the unaffected parts of the non-safety busses from offsite |
| power. |
| |
| The licensee notified the NRC Resident Inspector and state and local |
| authorities. |
| |
| * * * UPDATE AT 1956 EST ON 02/03/01 BY BOB CONOSCENTI TO FANGIE JONES * * |
| * |
| |
| The licensee has determined that one breaker failed catastrophically causing |
| the loss of one 4160 VAC bus and pieces of the breaker assembly caused |
| grounds in another 480 VAC bus causing its loss. The plant is stable in Hot |
| Standby. The licensee notified the NRC Resident Inspector. The Unusual |
| Event was terminated at 1544 PST. |
| |
| The R4DO (Blair Spitzberg), NRR EO (Richard Wessman), IRO Manager (Charles |
| Miller), and FEMA (Gene Nupp) have been notified. |
| |
| * * * COMMISSIONER'S ASSISTANTS' BRIEFING 1000 2/4/2001 * * * |
| |
| Briefer: Charles Marshall. Participants: Mamish (IRO), Richards, Wessman |
| (NRR), Dricks (OPA), Combs (STP), Hauber (OIP), Madden (OCA), Morris (EDO), |
| Levin (Chrm Meserve), Cain (Comm Dicus), Sharkey (Comm McGaffigan), Davis |
| (Comm Diaz), McCabe (Comm Merrifield), Brockman, Henerson, Kramer (R4). |
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|Power Reactor |Event Number: 37714 |
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| FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 02/04/2001|
| UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 04:25[EST]|
| RXTYPE: [1] GE-6 |EVENT DATE: 02/04/2001|
+------------------------------------------------+EVENT TIME: 01:18[CST]|
| NRC NOTIFIED BY: MATT BAKER |LAST UPDATE DATE: 02/04/2001|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DAVID HILLS R3 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(ii) RPS ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 A/R Y 96 Power Operation |0 Hot Shutdown |
| | |
| | |
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EVENT TEXT
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| AUTOMATIC TURBINE TRIP/REACTOR SCRAM DURING TESTING |
| |
| During performance or routine turbine valve testing, an automatic turbine |
| trip and subsequent reactor scram occurred due to low turbine emergency trip |
| system pressure. The unit is currently stable in Condition 3 (Hot Shutdown) |
| with reactor vessel water level being maintained by the motor driven |
| feedwater pump and reactor pressure being controlled via the steam bypass |
| valves to the main condenser. All systems functioned as expected. |
| |
| The NRC resident inspector has been informed of this event by the licensee. |
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|Power Reactor |Event Number: 37715 |
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| FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 02/04/2001|
| UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 14:52[EST]|
| RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 02/04/2001|
+------------------------------------------------+EVENT TIME: 12:45[CST]|
| NRC NOTIFIED BY: MIKE MEYER |LAST UPDATE DATE: 02/04/2001|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DAVID HILLS R3 |
|10 CFR SECTION: | |
|*IND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 80 Power Operation |80 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| DISCOVERY OF VALVE CLOSED THAT COULD AFFECT ACCIDENT MITIGATION |
| |
| "While performing troubleshooting operation on the Unit 1 Crossover Steam |
| Dump System an Instrument Air Valve was discovered to be closed, when it |
| should have been open. This closed valve (IA-1553) isolates Instrument Air |
| to the Crossover Steam Dump Valves rendering the system inoperable. This |
| system is required to be operable by the FSAR Appendix T and Power must be |
| <437 MWe if the system is inop. At the time of discovery power was <437 |
| MWe, however initial investigation leads to the conclusion that this valve |
| has probably been closed since October, 2000. Since Crossover Steam Dumps |
| provide protection for a Turbine Overspeed Accident and is part of the PBNP |
| Design Basis it was conservatively decided to make this 8-hour report. Unit |
| 1 will remain < 437 MWe until the system is fully restored and tested. An |
| investigation is continuing." |
| |
| The licensee notified the NRC Resident Inspector. |
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|Power Reactor |Event Number: 37716 |
+------------------------------------------------------------------------------+
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| FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 02/05/2001|
| UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 05:02[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 02/05/2001|
+------------------------------------------------+EVENT TIME: 03:15[CST]|
| NRC NOTIFIED BY: STEVEN KASPAR |LAST UPDATE DATE: 02/05/2001|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |BLAIR SPITZBERG R4 |
|10 CFR SECTION: | |
|DDDD 73.71 UNSPECIFIED PARAGRAPH | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 9 Power Operation |9 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| 10 CFR 73.71(b) SECURITY REPORT |
| |
| Safeguards system degradation related to detection/monitoring. Immediate |
| compensatory measures taken upon discovery. Contact the NRC Operations |
| Center for additional details. |
| |
| The NRC resident inspector will be informed of this event by the licensee. |
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